Hello friends,
Well let me start by saying this has not been my month when it comes to my Phantom. I bought and installed a Beholder Lite brushless gimbal for my Phantom and flew it and it worked great. I then opened it back up and got the tilt function set up and working. When I put the shell back on, however, the Phantom would not start up. I figured out the MC board was no longer sending out power so I bought and installed a new board. Once it was all hooked back up the gimbal no longer would stabilize... but that's a story for a different day.
I have upgraded the firmware to 4.02, reset to default parameters, ran an advanced calibration and calibrated all of my sticks. I also did a compass calibration outdoors. When I fly it now, it almost seems louder and squeakier than before. Also, it doesn't seem to hover in one place like it should. Is there something else I need to adjust since installing my new boards? I'll have to look at my gyro, acceleration and compass values after work tonight but I do know my MOD is around 1500... is that normal? If not, do I need to try the magnet trick? It's just been one thing after another lately and I just want to fly like I did before, without problems.
Thanks in advance
Well let me start by saying this has not been my month when it comes to my Phantom. I bought and installed a Beholder Lite brushless gimbal for my Phantom and flew it and it worked great. I then opened it back up and got the tilt function set up and working. When I put the shell back on, however, the Phantom would not start up. I figured out the MC board was no longer sending out power so I bought and installed a new board. Once it was all hooked back up the gimbal no longer would stabilize... but that's a story for a different day.
I have upgraded the firmware to 4.02, reset to default parameters, ran an advanced calibration and calibrated all of my sticks. I also did a compass calibration outdoors. When I fly it now, it almost seems louder and squeakier than before. Also, it doesn't seem to hover in one place like it should. Is there something else I need to adjust since installing my new boards? I'll have to look at my gyro, acceleration and compass values after work tonight but I do know my MOD is around 1500... is that normal? If not, do I need to try the magnet trick? It's just been one thing after another lately and I just want to fly like I did before, without problems.
Thanks in advance