A few questions, but first, the gory details. P4 with latest firmware / DJI-Go / Apple 6. Two routine flights - both ended with the RTH request. From the same location, 3rd flight -drone became unresponsive and flew away. A return to home was sent. The flight log shows the sent request. The playback says the drone hovered in place at a place that should have been visible by eye. I was walking towards that location when the low battery - RTH message flashed up. According to the flight log, the drone flew directly over my head and landed right behind me at Home. None of the 3 of us watching for it saw it after it flew off. The log shows a second battery low RTH message and the drone flew away from home and into a lake.
The log shows 18-20 GPS, good IMU and magnetometer calibration, but frequent loss of signal - is this common? Is it common for the logs to contain GPS data putting the drone in a place where it clearly was not seen by eye? There are several NaN entries for speed - is this common/normal?
TIA
The log shows 18-20 GPS, good IMU and magnetometer calibration, but frequent loss of signal - is this common? Is it common for the logs to contain GPS data putting the drone in a place where it clearly was not seen by eye? There are several NaN entries for speed - is this common/normal?
TIA
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