I have a P4P that had a pretty violent crash, it broke the gimbal arm and tore ribbon cables, broken the landing gear and bottom shell and the aluminum battery case. I have replaced just about everything including the gimbal esc board. The exception being the pitch and roll motor. I’m getting the gimbal motor overload warning and the camera won’t center and the camera rolls to a funny angle. I replaced the yaw motor according today droneteds videos. My question is, if the roll and/or pitch motor are defective would that affect the yaw motor? Or did I just screw up the yaw motor replacement when I switched the casing and need to try it again?