Ok, hey guys, i'm a newbie here, I know there are a lot of posts on gimbal issues but I couldn't find one that matched my particular issue so here goes. My phantom crashed yesterday, landed head first and my battery popped out, after doing my checks i realized that the camera was fine video and all, the app even says the gimbal is status is normal and I could adjust the pitch up and down no problem, however, when i test the yaw functionality it drops to one side and stays down and the gimbal status changes to motor overload. I have tried to calibrate it but it just starts and then says it cannot calibrate it. I checked the alignment of the motor and it was level but i still have the issue regardless, can anyone help me?
Here is a video of the issue-->
Here is a video of the issue-->