I recently had a minor crash because I did not lock a prop down entirely. In any case, I had not flown the drone at all at night until the night of the crash.
The sensors on the front and rear are saying ambient light too weak and are not working, however, the drone seems to make a weird hesitation when flying backwards or forwards and then will go. It also makes a weird noise like the drone is stuttering and then flys normally.
This originally led me to believe there was a motor issue after the crash, but I spoke with DJI and they said it was because the sensors are trying to work so the drone hesitates, then flies due to low light.
Any one else had this issue? I turned the sensors entirely off to test, and the drone did not hesitate or make the same noise, so I am curious if I have a bad sensor or they were designed this way.
Video shows the drone hesitating and the weird noise it makes.
Sent from my iPhone using PhantomPilots
The sensors on the front and rear are saying ambient light too weak and are not working, however, the drone seems to make a weird hesitation when flying backwards or forwards and then will go. It also makes a weird noise like the drone is stuttering and then flys normally.
This originally led me to believe there was a motor issue after the crash, but I spoke with DJI and they said it was because the sensors are trying to work so the drone hesitates, then flies due to low light.
Any one else had this issue? I turned the sensors entirely off to test, and the drone did not hesitate or make the same noise, so I am curious if I have a bad sensor or they were designed this way.
Video shows the drone hesitating and the weird noise it makes.
Sent from my iPhone using PhantomPilots