Hi all,
It sucks that my first post to this amazing resource concerns a P3A fail (I should really have posted sooner about all the stoke I've been having until about yesterday!).
I've been enjoying my new P3A (except the photo quality which suuuucks because of the blurriness, but that's a different post for another day) until yesterday when my attempt at follow me mode failed miserably.
Sitch: I launched my phantom as always, everything green systems go. Engaged follow me mode. Things looked okay on my iphone 6. I hop on my bike, holding the controller level and before I started moving the bird started acting erratically. Then all of a sudden seems like full throttle and into the bushes it goes.
It looked as if the GPS signal was less than optimal and the healthydrone confirms that. However, I would have expected the software to have recognized any significant deviations from the GPS and fail-safed somehow. Being new to this mode, I might have gotten it wrong somewhere.
Anyway, here's the log. If anyone would be kind enough to take a look and share what might have gone wrong.
Thanks in advance!
HealthyDrones.com - Innovative flight data analysis that matters
It sucks that my first post to this amazing resource concerns a P3A fail (I should really have posted sooner about all the stoke I've been having until about yesterday!).
I've been enjoying my new P3A (except the photo quality which suuuucks because of the blurriness, but that's a different post for another day) until yesterday when my attempt at follow me mode failed miserably.
Sitch: I launched my phantom as always, everything green systems go. Engaged follow me mode. Things looked okay on my iphone 6. I hop on my bike, holding the controller level and before I started moving the bird started acting erratically. Then all of a sudden seems like full throttle and into the bushes it goes.
It looked as if the GPS signal was less than optimal and the healthydrone confirms that. However, I would have expected the software to have recognized any significant deviations from the GPS and fail-safed somehow. Being new to this mode, I might have gotten it wrong somewhere.
Anyway, here's the log. If anyone would be kind enough to take a look and share what might have gone wrong.
Thanks in advance!
HealthyDrones.com - Innovative flight data analysis that matters