The other day I encountered some problems with the gimbal while the drone was in the air. Suddenly the camera started pointing down and I couldn't tilt it up with the RC dial tilt button. Got a "gimbal overload" message in DJI-GO. Checked it and noticed that two (the ones without plastic pins) of the white plastic worm-like things that holds the gimbal/camera had lost grip so the whole thing was unbalanced.
Been scanning the internet for solutions and find a couple of things I've checked. Like if the cables were off or if it had became misaligned. I couldn't find anything that appears to be wrong or broken on it.
When I start the drone the camera moves sideways but can't tilt. There's a buzzing noise when I move the drone. The camera becomes very hot.
I've been trying with some regular adjustments and checks on You Tube and various DJI forums. Been trying with 4 different Firmware. Been adjusting the gimbal from the app - It can only move sideways.
Starting to become desperate and about to send it to repair to DJI, or consider buying a new one - which I guess is about the same price from what I've read.
Before I do that I need to ask if there's anyone here that had the same problem and managed to solve it.
If so, please let me know how.
Been scanning the internet for solutions and find a couple of things I've checked. Like if the cables were off or if it had became misaligned. I couldn't find anything that appears to be wrong or broken on it.
When I start the drone the camera moves sideways but can't tilt. There's a buzzing noise when I move the drone. The camera becomes very hot.
I've been trying with some regular adjustments and checks on You Tube and various DJI forums. Been trying with 4 different Firmware. Been adjusting the gimbal from the app - It can only move sideways.
Starting to become desperate and about to send it to repair to DJI, or consider buying a new one - which I guess is about the same price from what I've read.
Before I do that I need to ask if there's anyone here that had the same problem and managed to solve it.
If so, please let me know how.
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