I checked again, all props are on the proper direction, the motors direction is reversed. I relplaced only the main board, did not touch the one for the motor
I bought a Zenmuse gimbal for my dji Phantom (with connection kit). I replaced the main board followed the instruction and video.
I have not calibrated by NAZAM Assist yet.
My problem is that after turning on the engines and increasing throttle the Phantom try sinking instead of lifting up...
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