Over the last few weeks I have been watching the jitter during the flight (video below) with my Phantom 4 Pro. I've tried everything to remove the bug - I calibrated the gimbal, IMU, controller, restore to default settings, upgrade to new FW v 01.04.0602, downgrade to previous FW. The flaw occurs even in good weather without wind. Do you now somebody what it is, how can I solve this? Do I claim my Dron? Thank you for your help...